Challenge
In July 2023, a leading oil and gas operator faced a critical challenge in isolating casing leaks within their well infrastructure. These leaks not only posed a threat to operational efficiency but also threatened compliance with the integrity requirements set forth by the California Geologic Energy Management Division (CalGEM). Previous attempts at resolving the issue through traditional cement squeeze methods had failed, leaving the operator in a difficult position.
Solution and Achievement
To address the persistent casing leaks and regain injection capability, the operator turned to an innovative solution—ReLine MNS. This advanced technology offered an alternative to the ineffective cement squeeze methods. The operator recognized that a new approach was necessary to meet the CalGEM integrity requirements and ensure long-term operational safety.
The ReLine MNS technology was selected to replace the series of failed cement squeezes. This decision was driven by the technology's proven track record in effectively addressing casing leaks and its potential to meet CalGEM's criteria. The chosen approach involved installing an approximately 800-foot liner.
The liner was successfully and safely installed in the well infrastructure and the isolated casing leak underwent a rigorous pressure test, witnessing pressures of up to 500 PSI over a duration of 30 minutes. This pressure test was a crucial step in ensuring the integrity of the solution and compliance with CalGEM requirements.
Given the uncertainty associated with the life expectancy of a cement squeeze and potential costs of subsequent squeezing, the operator realized the cost savings of utilizing an expandable casing patch as a permanent remediation solution that will last the life of the well.